So blew up my #3 rod. wondering what caused this. lack of oil, due to rpm? poor return? oil pump sucking air?
last time it was #2 rod. I really don't want to live with this again.
Motor specs,
Dual oil coolers with full flow plumbing
102 bore by 80mm stroke
long rods,
ham heads and valve train.
Running to 6800 rpm
g loads to 1.5
windage tray modified at pushrod tubes for oil flow
tuna can with 1/2 extra oil
Pics of horror below. First are this failure, then old failure.
What kind of rod is that? Looks aftermarket?
Odd that it's snapped in half and the cap bolts are snapped
Man that sucks!
I think the rod bearing seized on the crank. I see micro-welding on the journal. That happened before the rod broke.
Any warning? Weird vibration, change in engine tone? Anything?
Is the oil pressure stable in corners?
State of tune? Detonation can cause bearing failures. Bearing failures can break con rods.
I did get some warning (that I ignored) running hotter than normal, low oil pressure at idle, knock, etc.
I heard something happen part way through a run. but nothing visible outside. I knew better than to run it, but only 2 runs to finish the season....No detonation, running 100+ octane at 12:1 afr. this was a really fast motor. revved quick and put the power down. I figure close to 200hp and also 180ish torque.
Not trying to be a jackass . . . but sometimes it is what I do.
And we're discussing how/why this happened?
It does suck but when playing at those power levels and racing, this sort of failure shouldn't be a surprise. Especially when combined with ignoring the warning signs.
You have my utmost sympathy though. This is an expensive failure. But . . . racing is an expensive hobby. Ask me how I know.
On a more constructive note.
Play with this centripedal force calculator.
https://www.engineersedge.com/physics/centrifugal_force.htm
In this specific case, RPM's have increased from 5500 rpm to 6800 rpm. RPM is directly related to the velocity term.
The force on the rod bearings is going up as the SQUARE of velocity. Said differently, the force increase isn't linearly proportional to the crank journal velocity, it is increasing exponentially.
Double the velocity term in the calculator and watch what happens to Force, it goes up by way more than double.
Bottom line, although the top end was likely beefed up to control the valve float, the stock lower end rod bearing journals are getting overloaded. This squeezed out the very thin oil film that separates the rod bearing from the journal and prevents metal on metal contact.
First part of this occurs as dramatically increased bearing material wear. Eventually it results in steel on steel contact and the micro-welding Lew mentioned.
If you are going to run this type of engine at these elevated power levels I'd recommend that you do professional oil analysis after every race. If you establish a baseline immediately after engine break in, you WILL be able to tell when the bearing material is being shredded off into the oil more rapidly than usual.
At that point, you need to stop running the engine and replace the bearings at predetermined intervals. Ultimately you will likely get a crank failure in the long term after some unknown number of bearing replacements.
With the stroker crank, do a really thorough inspection/magnaflux of the crank, especially if it's a DPR or other built up then machined OE one. If it's a new forging it might have survived, but I'd be wary of a reworked OE. Had two DPR's fail on me due to the resulting closeness of the oil channel to the web after offset grinding. Went with FAT performance new forging crank after that.
I can't think of a motor with nearly a 4" bore that turns more than 6k.
Pushing an engine with low oil pressure and knocking sounds. Sorry but thats just dumb. As for what caused the failure I think Superhawk is onto a good lead. Sure a T4 can push 200 hp with some reliability but it will always need alot more attention and preventive maintenance than a less high strung engine. Changing the oil after every race with an oil analysis is a good start. Measuring is knowing. To me this isnt as much an engine failure as an maintenance/owner failure, the signs were there and you saw them and chose to ignore them.
I accept the responsibility for the failure. No need to run it in.
What I would like to generate is what to do to have a high rev engine live more than 20 hours? Bearing coating? Super secret windage tray mods? Better balance? Lots of folks build big bore motors, hopefully we can help them with longevity.
Regarding bearings, I’m curious why 6800 is high revs on a 4 and normal for a six. Are the bearings loads or stresses different! I always thought valve train was more the limiting factor to revving a four.
Exactly what I thought also. That the valve train was the weak point. I did address that. Let the high revers chime in.
Herb..
20 hours is pretty good for MTTF
were both engine failures at the 20 hr mark?
I see a sheared rod bolt...that is definitely a failure point on a high rev engine.
I will know more after the post. Engine is ready to drop. I should have it apart Saturday. Small thin bearing material in the sump. Correct on 1 sheared rod bolt. The other is ok, I haven't found the rod cap yet
All I Know is; Type Four Sale
oil temp was elevated due to the rod bearing failure. symptom of low oil pressure at idle and temps of 220 oil temp.
normally I run around 180 degree oil temp and 30 psi pressure at idle.
Also running 100+ octane race fuel at 12:1 full throttle and about 9:1 compression.
Thinking out loud here...Why are you running high octane fuel with a mild CR? With such low hours are your rings totally seated or are you pushing some fuel into the oil?
I had to rebuild two motors before switching to a dry sump due to rod knock. The CB Performance pump has pretty poor idle pressure, but is fine at anything about 1200 RPM. I did do a bit of work to open the ports in it...
Evan and I beat the piss out of the motor now (7000-7250 RPM) and it doesn't bat an eye.
actually my CR is higher, more like 10:1. I hate fuel knock. I would get some with running 93 so I just used 100 in this motor from the start.
How does the dry sump perform better if the oil is trapped in the heads and the issue is return flow? I guess you could tap a port in each head to help the return?
Don't vent the heads. Oil pools in vented T4 heads. The higher the revs the more pooling.
https://newsite.hamheads.com/2016/12/10/type-4-crankcase-breathing-system-tests-analysis/
Good read. Thanks Len.
For things to note, I did see my dip stick extend after runs. Seems to indicate excessive crank case pressure.
I did have the heads vented to a breather box that drains back. The dry sump and no vents sounds promising.
I employed Lens and Jakes work on the current motor. Heads are not vented and a -10 AN welded to the chimney that leads to a breather tank.
Len, just so I am clear, plug the head vents, don't cross connect?
Totally taking this off-topic a bit further...last few races I experienced unhappiness with my 914 regarding vented rockers.
Last summer with my 2L I was taking a nice long left-hander at Thompson (under the bridge) and the pressed vent tube in the right head came out. Dumped shad-ton of oil all around the bend, causing a couple cars to spin and one to hit the wall (I strongly apologized and ensured he did not buy beer or dinner that night). Field-fixed it by slightly swaging the tube, tapping it back in tightly, and gooping it with silicon. Held for the weekend.
This September at the Lime Rock Labor Day historics, using a borrowed 1.8L. The valve covers have welded 1/2" tubes coming off the valve covers with oil hose secured by hose clamps. First session out, driving through Big Bend and the left hose came off the tube....dumping a shad-ton of oil all around the bend, causing myself and several other cars to spin (no contact, thank goodness). Field-fixed by cleaning it all up, screwing it on as tight as I could, then drilling a hole across the hose, clamp, and tube and putting in a cotter pin, sealing it with silicon. Held for the rest of the weekend.
I'm also running a CB Performance dry sump pump.
I'm really getting tired of that. If I don't need these rocker vents then I'll just drill/tap/plug the holes on the 2L engine I'm building now and be done with it.
Attached thumbnail(s)
Curious...could unbalanced components accelerate the bearing wear and lead to this sooner?
Greg,
Just make sure that you increase the chimney vent some. I went with a -10 AN weld-in bung and a catch can to ensure good breathing.
-Aaron
I did run it to failure. Before this last event there was no indication of potential problems. I also had a couple of runs that were normal. From first indication, it was a quick failure.
I think my rod ratio was good, but will review my that was one of the changes with this motor. I had shorter rods previously.
To me 6800 rpm is really pushing the limits of a stroker T4.
You have a number of fail points that can be happening all at the same time, below I'm only addressing crank flex.
Crank flex the crank actually bending at/near the center main journal, as well the 2" "chevy" rod journals. Having 2 throws without support in between the rod journals is another weak point. the higher the RPM the more flex.
This flex is why a 1.7/1.8 case is a better choice over a 2.0 case, as the crank flexes even in a stock engine and it's hard on the center main case bearing saddle. VW knew this, basically stating a 2.0 couldn't be done reliably and it was Porsche that designed/modified the 2.0 crank for the '73 914. VW didn't use the 2.0 engine in the bus, till the 914 proved it was satisfactory reliable enough, for the 1976 model year.
With a longer stroke, in this case a 80mm, at high rpm you are amplifying all the bad, the crank flexes, causing bending stress on the rods, points of the bearings begin touching the crank journals, side loading, heat begins to spike, add into the mix events high RPM downshifting causing mechanical over rev, etc.
All of these stress points begin to cascade as RPM increases until the weakest point fails, in this case the rod.
I'd choose the 78mm crank with T1 rod journals just because the bigger T1 journal has more strength. I'd also lower my redline to no more than 6500rpm.
Hope this makes sense, I've got a L5 herniated disc back issues and I'm whacked out on pain meds.
Thanks Mark, I was hoping to get your insite.
Try whiskey? It helped with the pain of losing this engine.
Hope you get well soon..
When I had my heads reworked the machine shop closed/weld the breather vents is that a good or bad idea??
It sounds like it was a good idea.
Dat's purdy work up there...if you're bored and want to do another one...
Not sure that I want to pursue the Limited Prep HProd route. I already have the chassis at LP (it's an ex-ITA/ITB car) but the induction regs require using the stock, unmodified throttle body. That's a lot of development that has to be done around that one piece.
Colin Chapman was a genius. He would have gun drilled those bolts. I did at leat lop off the extra threads I considered using Jet Nuts to save some more weight, but didn't want to spend the money.
Greg, you ought to talk to Blake Meredith. He ran a ITB 914 and considered switching it over to HP. IMO it would be an expensive exercise in
The case work was a labor of love. And it worked great. That bottom end never gave a minute of trouble and ran 11 double weekends plus test days. Oil samples always came back perfect and hot idle oil pressures never changed one bit from new.
When I sold the car that engine was in it. Kip sold it to a guy in CA. I'd love to be a fly on the wall when he tears into it.
One thing no one else has asked is how were the other rod bearings. If they all looked really worn, then you should have a lack of lubrication. If they all looked fine, then you have another issue.
Engine is out, I won't have a chance to split the case until the weekend. Lots of copper in the filter along with thin pieces of bearing.
Herb, based on the picture of your crank I'd bet money your issue is oil starvation related.
You've probably had a lot of momentary oil starvation episodes that eroded the bearings over time till you suffered a seizure and failure.
FWIW, the prior owner of my car kept losing rod bearings due to oil starvation. It was an Improved Touring car, built in the late 90s. He said the problem began to manifest itself as Hoosier moved the (vastly improved) R3S03 tires...and ITx does not allow dry sump.
So he parked it in his basement garage with a spun rod bearing, built an ITS 944, and I bought the 914 from him 15 years later...
Oil starvation makes sense. More to come. The question will be how to address it without breaking the bank..damn, I was real strong this year. Keeping up with all the Caymans and gt's.
Herb are you running an accusump?
I'm of the opinion that an AX car doesn't need a dry sump system. A good tuna can and some mods to the windage tray are a big help.
Blocking the head vents will help keep oil from accumulating in the valve covers. That's a quart and half or more right there.
There are a bunch of little mods that can be done to improve the wet-sump function.
Properly engineering a dry-sump system is more complicated than just adding a dry sump tank and the plumbing. This is especially true if you are using a two stage pump, like the CB, which is a simple plug and play pump and adequate if proper prep is made, but not if you don't as the scavenge stage is not substantially larger than the pressure stage.
The mistake a lot of people make (I made it too) is to think that by adding the tank you can give short thrift to the scavenge aspect of the case prep. The reality is, you still have to prep the scavenge capabilities the same as if you were running a wet-sump system.
If you don't, when you corner and oil moves away from the pick-up you stop pumping oil out of the engine, but you don't stop pumping oil into the engine. This extra oil wraps around the crank and sloshes around in the case. With every significant corner you end up transferring oil from the tank into the crankcase.
At best this condition just robs power, but at worst it foams the oil so badly that even baffles in the tank can't de-aerate the oil fast enough. And if you vent the crankcase directly into a breather can and bypass the tank the oil that transfers from the tank to the crankcase will transfer out to the breather can.
The case mods I made to our dry-sump engines radically reduced the case-sump capacity with expoxied in place panels. The panels were arranged to direct oil to the pick-up which was down in my home made tuna can.
I also removed the goofy stud that runs through the pick up and cut off the restriction where the o-ring fits into the case. I welded a bung to the pick-up and sealed it to the case with a bead of silicon. The pick-up was secured to the bottom of the case with a bolt that went through from the bottom.
The stock by-pass circuit was sealed off with epoxy and an external regulator put in line.
[attachmentid=717974] [attachmentid=717977]
Nice, Len!
I, too, have been thinking about that sloshing problem, coupled to the fact that the CB scavenge pump isn't very much bigger. I've noticed that even when I let the engine run without cornering, there's always a lot of oil left in the case before I do an oil change. This goes toward explaining why.
Thanks for sharing this stuff; it's giving me a lot of thoughts.
Edit: Just walked out to the gaage to measure the CB pump: the pressure gears are 20mm long and the scavenge side is 26mm.
The CB pump is okay, but it has an internal cross over that can cavitate at high revs.
I used a Bugpack pump that came with 3 30mm gear sets and had the same cross over. I eliminated the cross over and one gear set. I did this by separating two gear sets with a hardened steel plate and shortening the shafts. This way the scavenged oil exited the engine through the cases original pressure circuit that originally lead to the stock oil filter.
With the external regulator I was able to dial in the pressure to a steady 50psi. That's not as much as most people run, but it's plenty of pressure. Observing the bypassed oil going back to the tank on the chassis dyno and comparing it to the scavenged oil returning to the tank I was able to estimate that ~ half of what was drawn from the tank was bypassed back, meaning that ~20mm of pressure side gear was plenty to generate a constant 50psi at 240* oil temps.
The modded Bugpack pump is on the left, the CB on the right. Once finished it fit behind the fan housing with only a slight bit of clearancing to a rib on the housing.
And yes, in case you're wondering, the old 10psi for every 1000rpm's is old school overkill. We ran 8300rpm's with 50psi for two years with zero issue. And on the dyno the difference between 60psi and 50psi was in the neighborhood of 5hp over 7Krpm's.
For a few years I circle tracked a 2.3 Ford mini-stock and ran over 8500rpms with 40psi and 275* oil temps. Never hurt a bearing though the oil temps did shorten valve spring life.
Some more pics.
Opening the scavenge port in the case to port match it to the Bugpack pump.
A better angle of the modified pick-up and the channel opening to direct oil to the tuna can.
Laughing at all the work that that goes into making a Type 4 hot rod. Truly a labor of love.
I live in a world where electric vehicles are quickly becoming more common. They don't have much soul as far as I'm concerned but they can be crazy fast and put internal combustion to shame in a street car drag race. Sad but true.
I have to wonder if someday folks will be swapping out IGBT transistors in an attempt to hot rod their 50 year old EV's as inverter technologies evolve. I have to say I doubt it.
Labor on and fight the good fight guys.
Love watching this post evolve and seeing Len's creativity at work!
I'm amazed at the work that went into this development...while simultaneously clearly understanding why Limited Prep Production is so attractive.
Engineering an EFI system around the stock throttle body suddenly ain't so unimagineable.
I do have and run a tuna can. I do not have an accusump. I like the ideas on the process of dry sump engineering! Not sure of my next steps, depends on what I can salvage. Don't think I will use a 80mm crank though.
But what a fun motor! Light up the tires whenever at full throttle. Pulled great out of corners, lots of lateral acceleration. I could finally keep up with all the modern cars, except the Tesla on autocross tires. Tesla's suck, but man do they accelerate fast!
The tires I light up are 225 45 15 Hoosier A7's.. it is a really sticky tire.
I am able to modulate the throttle to get the limit of grip.. They give up at 1.5 or so G's.
Motor is disassembled. See below for some pictures. Damage is not too severe, cam is ok, heads and lifters are ok. Case is a loss, 3 piston/cylinders look ok. crank is toast.
case GA000277 is history..
I have a 2L case you are welcome to.
Zach
Thanks Zach! I might take you up on that offer. I have one to tear down. Depending on what shape it's in I will let you know... Now if you only had an extra -6 oil tank.
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