Here is a link to part one:
http://www.914world.com/bbs2/index.php?showtopic=351117&hl=2056
I decide my t1 oil pump in my 2056 was doing me no favors with a smaller than ideal OD.
I still had the T4 oil pump from the 2.0 that was doing its job when I had a cam thrust bearing fail /knock, so I decided to pull it a part for inspection.
I will perform some measurements and get it cleaned up, if it turns out to be in good shape.
The pics look like a great core.
Agree - looks like a pretty good core.
Pin the idler shaft.
Mandatory reading:
https://www.thesamba.com/vw/forum/viewtopic.php?t=699156
Great link, this should be a sticky if its not there already
and a video :
https://www.youtube.com/watch?v=dJ_iKZHldNk
so what are your impressions of your observations pictured here? how many miles since it had been rebuilt, it seems like just recently you completed that rebuild?
Phil
Phil,
This build and the last build had a total of less that 100 miles the Failure again was the top end intake valves and guides. Ill post pic of the worn out valve guides
The bottom end seemed OK. but erratic oil pressure problems I am sure added to the guides issue
Also The Crank end play had .0045 when assembled and CHECKED
I added the rear main and the play went to zero . Sound like a familiar thread others have seen.... I continued any way thinking the seal was adding the buffer to the clearance. I had howling bear noises and the wear pic on the side of the thrust confirmed it was tight. Looks like new bearings and pump for bottom end I will check the saddles for possible line bore
Here is the worst of the intake guide #1. The exhaust guilds are fine at .001 t o .0015
This intake is at .006 to .007. This was only less that 100 miles and were NEW
https://www.youtube.com/watch?v=Y7KPNeAiRig
I have a new local shop add new intake guides and intake valves if needed
My summary of this build:
1) OIL pressure problems
2) Oil type problem ZR1 20w50
3) Temperature problems
4) Bad intake guides
or all the above
When she ran it ran VERY well power, speed no spark knock. FUN
Valvses would stick and dead cylinders till next run
Crankshaft float s/b .004" plus or minus .001".
One thing to do, to reduce the RMS potential for a leak, is to use the proper installation tool. Got away without using one before for years, but am now convinced of the value now (don't you hate having to drop an engine and transmission to fix a leak?).
Hear's why:
https://gowesty.com/blogs/article-library/flywheel-or-rear-main-seal-story
Here's the tool:
https://gowesty.com/products/rear-main-seal-install-tool?_pos=1&_sid=2653a61af&_ss=r
Best wishes for getting her fixed!
check in without seal and again once the seal is installed. should be the same.
0.0027 to 0.0051. most shoot for 0.004”
Place the thinnest shim in the center of the three shim pack.
Rear main seal tool, use a block of wood. Go easy and make sure it's not cocked, flush with the case. End play, shoot for .003.
GREAT info on the rear main seal. ..with mods
https://www.facebook.com/1160006259/videos/5098274283572774/
Happy day for a change in the garage
A world member set me up with a 4 post yoke for the engine stand (Thanks Nick)
What were your thoughts on the wrong oil? Why did you mention that?
From your picture of the engine case mounted in the new stand, you might want to do a little research to find a cure for the RMS leak problem.
Take a look at the posts in the Facebook "4th Dimension Type 4 Porsche/VW Performance Group" or do a YouTube search for Jake Raby's video about how to fix leaking rear main seals on Type 4 engines. I recently saw that video and was surprised by Jake's comments.
Raby files two very small relief passages above and below the rear main bearing saddle area on one side the engine case to allow oil a path to drain out of the cavity between the main bearing and the seal/crank spacers so the rear main seal stays oil tight. Raby says the factory oil drain hole is too high in this area, as well as lacking any way for air to enter the cavity so the oil can drain back into the sump, thereby creating an air lock which prevents the oil in that area from escaping unless it forces its way past the rear main seal lip. Raby also said that while the factory started using a drain hole in the 2 liter cases, it never put a drain hole in the earlier 1.7 & 1.8 liter cases. Raby further claims the factory's drain hole in the 2 liter cases was too small in diameter and located too high in the bearing saddle area to properly drain the oil back into the sump.
He also said it really doesn't matter what brand of seal you use (Victor Reinz or Elring) these days if you don't make the new oil drain passages he described in his video. However, Raby does mention that the black SABO brand seals are no longer any good and should now be completely avoided because the SABO factory's seal mold has worn out. Another thing he mentioned is that the width of the rear main seals is different because the VW Type 4 engine cases and the Porsche engine cases take different width seals because of the different sizes of the flywheel & pilot bearings in the two types of engines.
Raby said he now uses a proprietary rear main seal he gets from one of his customers who sells all types of industrial seals. Raby uses that "mystery special" seal on all the Type 4 engines he builds these days. Raby won't sell it to the public (nor does the Type 4 Store) and Raby said it comes from an unnamed military helicopter's drive unit.
I was thinking the VR1 20W50 was not the best oil for break in. Also may bypass the oil pressure controls to the cooler when cold and possibly longer with the 30mm pump.
Some-thing wore out all my NEW intake guides in less than 100 mile...
Total worn out!
I linked to the Raby live stream in post 19
Now that I'm on the stand I will cut the drains on the one case 1/2 but I did not have issues with my rear leaking. Thanks for descriptive tips...
Trying to keep the motivation up on this holiday week end....
Old trick of the trade...no one asks to borrow any tools!
This will be the third build?
Curious about breakin methods for the cam/lifters.
Rich
Rich,
Yep this is # 3 and the $1000 dollar question:
Do I reuse the Cam?
Do I reuse the Lifters?
Do I get new Lifters?
All new?
or all new and another cam profile?
first start:
http://www.914world.com/bbs2/index.php?s=&showtopic=351117&view=findpost&p=2939711
I will for sure show the inspection and be asking for advice as we get to this very soon...
The first run was with the supplied cam lube and 20 min burn in @ 2500 rpm with variation to speed slightly to keep the oil flying in all directions .Followed by tuning and re torque of the heads prior to installation in car... video in part one
Second time was the above cam and lifters ( matched to lobes and lifter bores in SAME locations) with assembly lube and 15 burn in @ 2500 rpm
Heads are repaired with new intake guides and 3 angle valve job (300.00):-)
NOT A CLEAN ROOM but good for measuring and inspection...
I have my fingers and toes crossed this motor purrs perfectly for you.
I will be having a sale on engine parts it it doesn’t... Thanks for the Positive motivation
I did some detailed measuring on the con rod journals, but instead or re writing, Ill post a link
https://www.facebook.com/groups/type4ever/permalink/3393206420997827/
Lots of great info on this thread! Good luck!
It took a while but I finally got a set of NOS KS/KW 0.010 main bearings on the way....
I did have to pay more than I should have....but I think I am worth it! ;-)
Thanks to the generosity of a Kerry, world member here (White1975) and the loan of a T4 timing gear puller. I have the old bearings off and will be ready for the new bearings when they arrive
WooHoo
Add a VDO HEAD TEMP thermocouple under the #3 spark plug. Milled a small hole for the wires and crimp.
Unless things have changed, the VDO head temp gauges are not good, and are not temp compensated. I'd strongly consider using a quality head temp gauge like the Dakota Digital (or at least a temp compensated gauge.)
Milling a hole like that is, IMO, not better then cutting a groove in the boss for the K type sender. And when you decide that you are tired of the VDO CHT lying to you and want to change it out for a better one, you are going to be very unhappy when you go to remove and install a new K type sender.
Zach
This way the sensor stays in place when servicing the plugs. Clean and EZ. IF this was a 2.0l FI head, a grove should be the way I would have gone too. It was simple to install by pulling the terminals out of the connector. It should be serviceable with the tins in place with long tiny bent hemostats or pliers
Thanks for the tip on the Dakota. If they made a matching gauge for my console I would give them a try but at this point I’m all analog and Black /White (no digital) VDO is beter than running blind
Just got a new tube of valve lapping paste...The old one lasted 45 years!
Tonight lapped the cylinders to the heads(no head gaskets). I did not lap last time but did have the heads fly cut each time to true.
The new intakes were recut (machine not stone) and new guides. Owner of the shop said. These will be much better than the old valve jobs. They lapped the intake , so I decide to lap the exhaust too. Look good.
I ran a thread die on all the case studs and pullout all the plugs to clean with a gun cleaning kit prior to final cleaning . Lots of cleaning , then lots more
KTM 125 top end upgrade in the background.....while at it for my son.
You keep learning all sorts of fun things!
heads are disassembled cleaned and lubed and back together. ready to drop on...
The windage tray had the same old seals, so a new set glued in place and ready for installation along with the cam bearings. USING A DOUBLE THRUST and setting the endplay at .002 inch flipping the bearing without out the tab 180 degree got my play set about right. The 2 shells work working against each other and canceling out he endplay important to test the play on both half and Assembly to ensure you have it just right
here is a video of the camshaft end play
https://www.youtube.com/watch?v=WpUDEaOWWa4
Measured the case, bearings and crank journals as well as plastic gage the split shells.
Case is sealed and about ready to jugs and slugs...
Can't wait for this to be fired-up.
I did pin the shaft on the T4 oil pump. Drilled and milled a 3/32 hole in the housing and when I hit the hardened shaft I switched to an end mill. That shaft is hard so it just left a small mark. NO problem. A aluminum punch and hammer the shaft press out EZ. To EZ! I would pin every one of these moving forward .
With the mark I was able to grind a slot in the shaft for the pin to fit about an 1/8 inch deep with a cut off wheel. Then tapped the hole for a set screw-in the housing. Then cleaned and red lock tight the shaft back into place so the slot is seen in the hole. Intall the pin to full engagement with the new slot with more red lock tight. Installed the set screws so the pin would not come out (more red lock tight) and staked the set screw in place.
I feel confident that this pin and set screw are now part of the housing and will not come out.
After thinking about the for a moment I should have just welded the pin in place like a short barreled muzzle brake...good enough for the ATF as permanent!
Sorry no pics or vid
Playing with a thermal dispersion paint from Cerakote (transfer Gray)
Here:
http://www.914world.com/bbs2/index.php?showtopic=366063
heads
Lapping the heads can only be a good thing, and you get a chance to look at the cylinder bores and pistons/rings too. AS well as resealing the case to cylinders while you are at it....top end work should go pretty EZ for people with good repair skills, even if they are new for type 4 work...Just need simple hand tools and a torque wrench and some hi temp Curel T(green) or a small dab aviation sealer ...What could go wrong....
-Cheers.
and thanks for the support
I updated ALL my videos on You tube for Robert Finegan to public...so you can take a look with out all my descriptions and chat...
@robertfinegan4491
https://www.youtube.com/channel/UC6Ol_gbz9D5RPLqpYPD2qCg
https://www.youtube.com/@robertfinegan4491
Tonight I cleaned the carbon off the piston tops and got everything ready to install
Piston rings lubed and skirts and pins and started assemble .
Problem:
The new engine yoke did not have enough room to install piston pin # 3. #4 is installed first on the right side because the oil cooler is there and the pin is installed from the rear/center of the motor. When I got to # 3 the pin would not clear the engine yoke and I had to set it down and remove the yoke and install the pin/cylinder assembly. 10 extra minutes so not be deal .
Starting to look pretty good....
one more
Looking really good, Robert!
Thanks Rob, Thanks for positive feed back, it is greatly apreciated.
-Robert
Thank you for doing such a great job documenting best practices.
Wonderful way to help the rest of us.
TLDR,
Did you use that paint on everything?
Cool.
I request a 1/2 year update on the paint please.
plan for the weekend...
1)Home made Jet Doctors for IDF 44
2)Torque heads and head tins
3)Paint Push rod tubes satin Black and install lifters
4)Valve train and valve lash/covers
5)Time permitting..stub pipe installation
Continue R/D: pressurized engine priming tool/system
...lots more to come
Darn, the engine yoke got me again. its touching the # 3 cylinder. I need to pull it off again and make a slight grinder modification to the mount so it now longer touches and I can torque the head.
However i did make good progress and I have another day to get back on track... I get a pic later to show how I did this.
until then..
DIY: Jet Doctor for idle jets or just by them from CB
I picked up some 3mm or 1/8 brass tubing from the hobby store and I did some calculations of how high to make them.. it turns you the main jet stack on my carbs are 1.950 from the bottom of the top plate..( I guess 2 inch would have been fine) but mine are he SAME height as the main stacks. IF its good enough for Weber it should work fine for the Doctor...
MY old Italian Webers had short stacks even with the top plate..I need to change the too, I guess?
1) I cut 4 piece of tubing to the correct length (1.950 inch)
2) I flared the end of the base wit ha automatic center punch to gain a snug fit in the top of the carb vent hole
3) Add some 515 gasket sealer to the hole
4) Tap and set the brass tube it to top plate till flush on the bottom of the casting
5) Repeat for the there 3 vent holes
All that is left is a few holes in the gasket and to drill 4 holes into you air cleaner base
-Cheers
https://www.youtube.com/watch?v=boURpJiAvZk
cylinders hitting the the yoke frame
Today I installer the blower housing, blower front tins alternator, belt left tin, intake...
Wanting for a Distributor drive spring before installing the right tin (tues)
Installed and torqued Clutch, Pressure plate and front Blower with blue loc tight and Alternator a with belt with front tins
Today I recondition push rod tubs to remove dents and reduce diameter for clears to stub pipes
tightest clearance is #1 and #4 exhaust to stub and then 2/3 to exhaust
https://www.youtube.com/watch?v=xx6OP91X9rU
I may have to try to fit an aftermarket thermostat. The header is too close for the stock on to fit. I hate the new one fails in the on position though!
Yeah getting close. about time to remove the OE engine and test the oil prime and final valve lash.
Good eye. Not wanting to pull the alternator/cover I have been putting this off. I decided now with your comment, to pull the terminals our of the connector and install a seal/bushing. It was not as painful as it sounds with a terminal too. Seal from Hot air and no chances of cutting or grounding my charging system.
This week starts the removal of the OE and trans. wit the Lift plate from Tangerine and fast jacks this will go quick. Done wit the test runs of my make shift engine oil primming system. With a regulator I can control the oil pressure and feed rate,. Negative: If I run the tool empty I get oil foam and air. SO small batches of prime 30 weight break in oil.
Add a PMO fuel regulator (purchased in the classified here) I made a mount to the case and insulated with silicone 1/8 washers (think GM HEI button) so heat should not be much more that engine compartment ambient temps. COOL recirculating fuel! Woo hoo. SS lines to the carbs carbs and once I'm up and running will look at the Tangerine SS tunnel lines
Waiting on some 6an to 8mm fuel parts..later today
Cheers
install pics..all done under the car.
including Wide band O2 and tangerine Evo muffler
another view of the Tangerine clutch mount Gen 1
no more melted cables
Lets see how I did...
I add 5 gals of 93 octane to the tank after draining it with the stock fuel pump. this worked great wit the ground wire on the relay to run the pump when the key is one.(carbs)
Topped of the oil to full 4 qt with tuna can
Key on and checked new plumbing for NO leaks and 3 psi
SO FAR SO GOOD
Lets see if it will light off
2 pumps on the accelerator to prime pumps and got shots of fuel
KEY on and Contact....crank..crank crank...no fire
again Crank crank crank crank..no fire
pump pump crank crank crank...she is not going to go!
A quick check I found NO SPARK for my Malory
SO...
I think I spiked the module doing power balance test by pulling plug wires last time it was running.
I had a no start and then it cooled and ran again..no nothing
I hooked up a 009 points distributor and a ground wire...
Gave it a spin...and ZAP, ZAP, ZAP!
Pulled the Mallory and borrowed the 123 from the Djet
Dropped it in without changing the last clamp position (ran at that setting)added the power connections and plug wires etc..
Pull the coil wire and add the stark tester
Key on"Crank crank crank = ZAP ZAP ZAP
HERE WE GO AGAIN:
2 squirts on the accelerator
Crank, cra.... VAROOM!
up to 2,000 PRM and synced the low Slave carb.... 15 Cam burn just to keep the oil pumping
60 psi
running good for 5 mins
set base timing to 10 degrees and continued the BURN for total of 15 min
Idle at 1000 and oil at 20 psi (HOT) well pretty warm
AFR 12.1 at 2K rpm may be a little rich but Looking good
Head temp at 300-340
Will tune a little more Sunday and swap out the start up oil and reset the valve lash to about .001
HERE is the proof: I did set the valve lash a little loose @ .003 so a little noisy
https://www.youtube.com/watch?v=yBEDdvhwzNU
Nice job, Robert!
Excellent!!
Congratulations! She sounds good.
Sounds healthy!
Pretty balanced for a first start as well.
I'm a huge believer in running it under load (driving) for the first couple of hours.
Medium acceleration but using compression braking whenever possible.
Trying to achieve the highest manifold vacuum I can (engine decel).
I'd want to drive it this afternoon!
I'm happy for you and a bit envious...
My 2055 is a few months away.
You might need those smaller idle jets you have!
For no load 2K I'd want to hit north of 13.5 and south of 14.5
I add a new Malory Module to my ignition system Hi fire and I have to say ...AWESOME
Dropped it right in at my OLD setting. One tap on the accelerator COLD START...Vroooooom
NO long crank or stumble. Great idle too.
Getting Better...
YES I will get the base timing set (10-12*)and limit the advance to a bout 16 degrees shooting for the DESIRED 28 total
It should be cool this weekend. 75 in the morning, so I l drive around on the idle Circuit and gets som Wide band numbers
30 min or so run time so I better get some Fresh oil in it too...LUCUS 30 weight break in oil
On a first run in like you just did I clean the piss out of my drain pan, drain oil into it.
Let it sit for hours, poor the top 95% off and "pan for gold" with the remains.
Shine a flashlight through it....
Any bad glitter and I'm pulling it back out...
It's so much cheaper to fix if you catch badness early.
I wouldn't do an oil analysis until after I had 10K on the new motor.
Fresh oil (lucus 30w break in oil) and now hit the 100 mile mark.
I am waiting now on the Redline jet-pac for mains and air correction jets. It will be here for the weekend and a few jets from Cb that are not in the kit.
Head temps are under control (WOOHOO!)stable just under 350*f. It only breaks the 350 mark on spirted pulls and come right back down. Cruise is 325 -340*f
DID I say is 95-98 degrees here in NC wi h HIGH humidity
I will share the carb jet specs once I get the lean hole tuned out.
the Innovate LM1 is working fine. but NOT the Data Logging
Any one have the OLD Innovate Logworks 1 or 2 cd? The Log works 3 Crash on use with the Download of the log files
data logging would make this thing AWESOME
NOTE: Did any one tell you the thinner 30W oil will cool better than the thick 20W50?
I am running head temps around 230 on a hot day in NJ. Oil pressure is 78 lbs at start up and 38lbs at 3000 rpm hot. Running biral cylinders and Driven 15w50 oil. 30w may cool better, but what about oil pressure?
for those not familiar with CHT ..this from Raby QA
What is a normal temperature range for a Type IV engine?
Generally head temps are desirable below 365°F. I like heads to run 265°F-365°F as a norm. 375°F -395°F is getting warm, with 405°F being too hot for any sustained period of time. Oil temps should run 180°F-220°F, as an optimum. 225°F-235°F is warm and 235°F+ is hot and should
WRT the Mallory module. I'd suggest not only adding the Mallory Circuit Guard, but also a ballast resistor to drop the voltage to the module. It was only after I had both that I stopped losing modules.
I second the Mallory circuit guard and ballast resistor.
This about where I am at too for CHT
My oil is 210 to 220 about straight up and down
Tuning the 40 IDF 32 vents. Still running a bit rich but my temps numbers are very good at 335-365 and peaks to about 375
I did have to drill some jets to get in between numbers
Base line timing @11* and all in at 3000 for total 29*
accelerator pump rod at 6.5 mm
idle jets 57
f11
main jets 137
corrections 210
wot is still 12.2 to 12.6
next try will be:
135 mains and 190-200 air correction
rich hole air 3200 to 3400 still in transition circuit and mains coming on
She will pull STONG if you let her...
Lm1 not logging?
Can you describe the hardware?
Is there a plug? Are you using a laptop?
Rich
Seems to be a known issue with the logworks 3 application
There is a function to download the saved log files from the old lm1 recorder/display
This worked on the older logworks 1 and logworks 2 running xp or vista
the newer software crash on download of the log files and innovate did not fix in the newer version logworks 3
I can get an old PC but not finding the install cd / download for the older log woks app/interface
While waiting on a 57 idle jet, I pulled a plug to check how its burning...
...it has a nice tan!
What are you Mallory guys using for spark plug wires?
I have the red 8mm Malory plug wires, but they will attach to the VW OE distributor cap too
Today I installed an Older version of the Logworks3 software on a VM for XP (vm ware studio.) The old version was found in Way back machine for 2012 and is WORKING. It DID Not work on Windows 10. I was able to get 21 logs from the device and will clear the old (PO) logs and take my first recording of the AFR and with a bit of luck an RPM cannel too. I had to rig my inductive pick up to a 3.5 mm Audio jack input to the PRM adapter and analog adapter cable
Progress on the data logger and 57 idle jets are on the way. Hand drilled .60 were too BIG and .55 had a big lean hole in the transition at 3-4 k rpm Pop. Pop Pop and 16:1. I open my idle mixture screws another 1/2 turn and the Pops are gone. running pretty good and hands off the tip in pretty good.
Mains are reading 12:5 t o 12.8(1.30) for WOT and leaning out a little more as redline approaches . Trying real hard NOT to see REDLINE. But pulling a quite bit Higher and longer Into the upper rpm ranges 6K +. :-).Not just making more noise, but still pulling harder as it revs....(on the BUTT DYNO). Double valves springs will handle this No Problem
200 + miles on break in and leaks have been found and fixes
FWIW: I had to clean my speedo head of grease from the cable lube years back that made its way up to the head and the Odometer gear was slipping. ALL set and working very well and smooth again. That junked things up pretty bad and the needle/pointer was not returning any more
My first log....The last downward slope is the mains coming in at 35- 4500 rpm and look good at 13.2:1 and richening slightly (1.30)
I think I see the lean pop pop pop at 2-5 sec. (55 idle jets)
Here is an odd observation
While warming up the first light throttle up into the transitions feels smooth and no pops. try it again in a few seconds or another gear and is lean
Some times the ratios feel look good some times they are lean
I am going to have a helper watch my fuel pressure gauge on some next recordings
I did read somewhere that the fuel enricher (choke) gave some users problems rich or lean (not sure) that are not hooked up but the valves are in place.. I have seen dummy valves tap took off the ports (X4) with no holes.. 15-17 bucks each
I have richened the mains to overlap over the transition circuit and felt a little sluggish rich but not great numbers on the mains and WOT. But no lean hole or pop pop pop. I feel I’m on track with the correct 130 to 135 mains and richening the ideas to .57.
.60 Idle jet was very rich and 55 too lean
Fun to see how thy work
MORE LOGGING FUN TO COME
FIRST imported graph after a little smoothing
My RPM was off but working so I need to rewire my adapter on the 3.5 mm audio jack
I did get the RPM input working for the inductive 3.5 jack
Set the range for 0-1 volt and the rpm seem to be spot on now
woo hooo
another small win
FWIW:
It was 2 years ago today I was driving the gen 2 2056 for it short lived 50 miles....
Good job getting this sorted Robert.
Rich plug soot is due to idle screw out to give more air fuel to richen the lean hole at top of transition
The tan is the wot and the 13.2:1 as its leaning out a the end with the 130 mains with f11 emulsion tubes
Agreed the 55 idle jets are way too lean
I will post the graph of the new .57 idles some time tomorrow
The right margin is the key and the curser value under the mouse
new jets for idle .57 came in today..still too rich so back to the .55 and a data log snapshot recording
40 pdf
32 vents
55 idles
210 air
1.400 mains
29* timing at 3000
next move it to 220 air
single pull to 3600 rpm
Note the dip rich at the end is the main jets 140(rich) coming in.This was to show where the lean hole is and will continue to add air correction till the lean spike is gone...
Too rich?
Are these WOT pulls?
Are these pulls? I mean are these under load?
all data logs are while driving
Saving WOT for last but I am feeling the main pull hard at 3500 rpm
I will add a degree or 2 (+-) now that it is no longer running rich and see how the temps and performance base line again...
more fun with Logworks 3
https://www.youtube.com/watch?v=_2f9yGM7hhY
https://youtu.be/_2f9yGM7hhY
Is the blue line the old and the dark line the new? I think you might be reversing the terms... It was running lean, if I am reading that correctly. Now it looks really nice, and rich enough not to blow your engine up
I'm still sitting here trying to figure out what is on the graphs.
On the last graph with the purple and Black lines...
Is Purple AFR and Black RPM?
Or is purple and old run and black a new run?
You need to have a line on the chart that shows RPM somewhere. It will help a LOT with tuning.
Zach
Is Purple AFR and Black RPM
0-7000 rpm Black
0-22 afr Purple
all the runs or recording sessions are in its own tab
This shows a gradual pull ”driving” from first gear and 1000 rpm to about 3500 rpm for a pull on the main jets for about 5 sec 1/2 t o 3/4 throttle pedal .
I thinks this is followed by a shift and cruse in second for a time at about 2500 rpm
Followed by a shift in 3rd at 2000 rpm cruise ( 1 min mark) and gently drive away...
( I think, I need take better notes..it may be just a single pull and a gradual cool down and no shifts just a first gear pull?
emerygt350
yeah its looking pretty good
I have been playing with a PMO fuel regulator. The gauge says 3 psi and stays steady, but the feel you get is it fine driving and the hand off from transition to main is smooth and the next time time I get into it it seconds later feels like there is not enough fuel. if I can not get this sorted, I will put the CB/Tangerine 3 psi pump back on with no fuel return
no work last night for bowling/drinking beer.. High game of 223 and 605 scratch series (WOOHOO)
Thinking, reviewing data logs and clearing my head...rain this week end, I may run a quick errand and get some more test data
The dash board and the graph are the same session
I would be super scared of those values, particularly down low too. Up high it can get wonky but I would be shooting for nothing ever touching even 13 during a WOT pull. Between 3 and 4k is when these engines are really building their power and you are running super lean at that point.
Only time I want to be at 14.7 is cruising under very light load.
FWIW< I’m trying to get the lean spots out of there..
13.1 across the board and maybe touch 13.9 /14 on light cruise
Now that I understand the log, that is pretty cool. Good thing you got it working again. Is this Wot pull in first or 4th? Or are you shifting?
I think it might be best to keep it in a gear like 3 or 4 and go from 1k to 5k
Zack
thanks for the tip...ill try another if the weather hold out today
11 afr is too rich for me...
Those look a lot better. Its better to be on the rich side then the lean side when you stomp on it.
Get a log just driving around how you usually drive the car and compare WOT to normal driving. Do a log just cruising with low load.
Zach
Yes, this looks much better and the daily driving log would be great. I would be nervous about those lean parts of 3 to 4k, that's where the fun is and often the point at which the engine is under the greatest load, I would rather be at 12-13 there. Even my water buffalo mustang keeps it around 12.5 under that kind of condition.
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