Home  |  Forums  |  914 Info  |  Blogs
 
914World.com - The fastest growing online 914 community!
 
Porsche, and the Porsche crest are registered trademarks of Dr. Ing. h.c. F. Porsche AG. This site is not affiliated with Porsche in any way.
Its only purpose is to provide an online forum for car enthusiasts. All other trademarks are property of their respective owners.
 

Welcome Guest ( Log In | Register )

> compresion issue in a 1.8, low on no. 4
broomhandle
post Aug 20 2012, 11:11 AM
Post #1


Member
**

Group: Members
Posts: 290
Joined: 26-June 09
From: Half Moon Bay, CA
Member No.: 10,512
Region Association: Northern California



I have a 1.8, and it runs like a bus motor, its a EC 1.8. i can be driving and it will be a 914 for a few seconds and then back to a bus...

so, i did a compression test

4= 80-60
3= 100
2= 120
1 = 100


and my plug on no. 4 is black.

new plugs.

what could be going on?

the valves are not adjusted. and also, i feel like its timed right. but, then you drive it.... and it just not timed right...

what could be going on with No. 4? and why would No.2 be higher? because its the opposite side? compensate?

im a lone 914'er... and Vdubber... you guys are the only people to ask! (IMG:style_emoticons/default/smile.gif)
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
 
Reply to this topicStart new topic
Replies(1 - 9)
aircooledtechguy
post Aug 20 2012, 11:55 AM
Post #2


The Aircooledtech Guy
***

Group: Members
Posts: 1,966
Joined: 8-November 08
From: Anacortes, WA
Member No.: 9,730
Region Association: Pacific Northwest



It sounds like you have 2 un-related issues going on.

You NEED to do a proper valve adjust on the motor BEFORE doing a compression test. The motor also needs to be warm in order to get accurate readings. Pull all plugs and hold the throttle wide open while you crank it. Low readings can be from leakage at the valve or past the rings. If you have oily goo on the plug and a valve adjust doesn't make things better, I would suspect the rings.

The black plug could be from a few other things too:
1. bad injector; sticking open?? Easy to check. Pull the injectors and run the fuel pump to see if it leaks.
2. intake/exhaust valve seat coming loose. This will cause it to run poorly (intermittently) and explain the low comp. # on #4. Dangerous situation since when it fails, it junks the whole motor. You will discover this while doing that valve adjustment you need.
3. Vacuum leaks. Use a can of carb cleaner and spray around ALL joints/seals in the intake system. If the RPMs raise, you have found a leak. Do not stop looking if you find a leak, as there may be more than one.
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
timothy_nd28
post Aug 20 2012, 12:04 PM
Post #3


Advanced Member
****

Group: Members
Posts: 2,299
Joined: 25-September 07
From: IN
Member No.: 8,154
Region Association: Upper MidWest



The bad plug, is most likely a failing non firing fuel injector. It explains what he said earlier about the car driving like a porsche sometimes and other times like a bus.
You must adjust your valves, and warm the engine up before doing any compression tests.
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
broomhandle
post Aug 20 2012, 01:20 PM
Post #4


Member
**

Group: Members
Posts: 290
Joined: 26-June 09
From: Half Moon Bay, CA
Member No.: 10,512
Region Association: Northern California



it has a 32/36 weber.
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
timothy_nd28
post Aug 20 2012, 01:53 PM
Post #5


Advanced Member
****

Group: Members
Posts: 2,299
Joined: 25-September 07
From: IN
Member No.: 8,154
Region Association: Upper MidWest



Damn, anyways, I had a bad injector a month ago, and that's how my plug looked. Start with the compression check
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
broomhandle
post Aug 20 2012, 02:01 PM
Post #6


Member
**

Group: Members
Posts: 290
Joined: 26-June 09
From: Half Moon Bay, CA
Member No.: 10,512
Region Association: Northern California



ill start with a valve adjust. any easy way of going about?

just drop the engine a bit, and loosen up the trans mounts?


i wish i had a lift.... (IMG:style_emoticons/default/smile.gif)
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
LotusJoe
post Aug 20 2012, 02:31 PM
Post #7


Europa Twink Driver
**

Group: Members
Posts: 406
Joined: 30-November 09
From: Southern California
Member No.: 11,085
Region Association: Southern California



QUOTE(broomhandle @ Aug 20 2012, 01:01 PM) *

ill start with a valve adjust. any easy way of going about?

just drop the engine a bit, and loosen up the trans mounts?


i wish i had a lift.... (IMG:style_emoticons/default/smile.gif)

Loosening up the motor mounts isn't going to get you much room. There should be enough room. You may have to remove the heater piping going into the exchanges, but that's about it. It's cramped but there is enough room.
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
brant
post Aug 20 2012, 10:33 PM
Post #8


914 Wizard
**********

Group: Members
Posts: 11,640
Joined: 30-December 02
From: Colorado
Member No.: 47
Region Association: Rocky Mountains



it could be that your motor is just shot...

but that is the bad news
its worth doing a valve adjustment and maybe leak down to know

buy a haynes manual and its relatively easy with a jack and jack stands.....

or go to pelican and print a how to article at a minimum.
User is online!Profile CardPM
Go to the top of the page
+Quote Post
broomhandle
post Aug 21 2012, 10:34 AM
Post #9


Member
**

Group: Members
Posts: 290
Joined: 26-June 09
From: Half Moon Bay, CA
Member No.: 10,512
Region Association: Northern California



QUOTE(brant @ Aug 20 2012, 09:33 PM) *

it could be that your motor is just shot...

but that is the bad news
its worth doing a valve adjustment and maybe leak down to know

buy a haynes manual and its relatively easy with a jack and jack stands.....

or go to pelican and print a how to article at a minimum.



yep agreed.

im going to do the valves, new gaskets and check the head bolts.

after that.... if its a no go. im done with the motor, a rebuild maybe or just done! (IMG:style_emoticons/default/smile.gif)

User is offlineProfile CardPM
Go to the top of the page
+Quote Post
brant
post Aug 21 2012, 11:23 AM
Post #10


914 Wizard
**********

Group: Members
Posts: 11,640
Joined: 30-December 02
From: Colorado
Member No.: 47
Region Association: Rocky Mountains



unfortunately you can't do the head bolts without dropping the motor and stripping the tin.

but they would be fine anyways.
so let us know what you find out from the valve adjustment, retest.
User is online!Profile CardPM
Go to the top of the page
+Quote Post

Reply to this topicStart new topic
1 User(s) are reading this topic (1 Guests and 0 Anonymous Users)
0 Members:

 



- Lo-Fi Version Time is now: 10th June 2024 - 05:31 PM