OK...
Karl, thanks for prodding me to take the pics. It forced me to tackle it one more time. It's out (with no help from Stitch... probably why it didn't take too long! HA)
The joint under the dash was the culprit. It was totally undone and loose. It was just binding there. I reached under the dash and tapped it with my pry bar (honest... I just tapped it) and "clunk" the rack hit the floor.
No pictures on this thread. I'll post another showing the dismantle and the Turbo Tie Rod install.
Couple of ?'s:
1. What have you guys done to tighten the Turbo Tie Rods. Looks like a thin 31mm. Should I just grab an el'cheapo and grind it down?
2. Anything I should do to this rack while it's out? Part of me wants to dig in and relube it etc... but prior sources say not to touch it.
??
Thanks!
E.
(I'm actually doing something today!)
P.S. Karl... gotta love the glass bead blasting cabinets huh?