Home  |  Forums  |  914 Info  |  Blogs
 
914World.com - The fastest growing online 914 community!
 
Porsche, and the Porsche crest are registered trademarks of Dr. Ing. h.c. F. Porsche AG. This site is not affiliated with Porsche in any way.
Its only purpose is to provide an online forum for car enthusiasts. All other trademarks are property of their respective owners.
 

Welcome Guest ( Log In | Register )

> Dyno Time, light dyno run clears smokey 2.4
phillstek
post Apr 5 2012, 03:20 AM
Post #1


Member
**

Group: Members
Posts: 350
Joined: 19-May 10
From: Byron Bay, Australia
Member No.: 11,741
Region Association: None



Recently started the engine after not being run for 12 years only to discover that it was blowing massive amounts of blue smoke.

After seeking and getting good advice from world members I decided to run some Liqui Moly Engine Detox in it to see if that would loosen the stuck rings. The instructions advise getting the engine oil hot, adding the detox and letting the engine idle for 15 minutes before draining the oil.

As the car is not road registered yet we decided to run it on the Maha dyno instead.

After initially getting the engine to operating temp we then proceeded to load it up on the rollers and bingo, after about 5 minutes of running it up the rev range....no more smoke and the oil pressure rose and held well.

I didn't bother using the additive at all. Spent the next hour or so setting the mixtures AGAP and then all of a sudden the engine backfired massively, died and wouldn't start again. The backfire was so loud it brought all of the techs from other parts of the workshop to see what had happened. I thought we killed it judging by the look of the dyno techs face.

We traced the cause to the points which were also 12 years old and not opening properly. After pulling the dizzy and dropping a new set in she fired up again straight away and idled smoothly at 800rpm with only some minor popping and farting when transitioning from the idle to the main circuits.

So she will be returning home soon for final assembly and registration.







Attached thumbnail(s)
Attached Image Attached Image
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
 
Reply to this topicStart new topic
Replies(1 - 3)
nsr-jamie
post Apr 5 2012, 04:12 AM
Post #2


914 guy in Japan
***

Group: Members
Posts: 1,182
Joined: 7-November 07
From: Nagoya, Japan
Member No.: 8,305
Region Association: None



how much power did you make?
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
phillstek
post Apr 5 2012, 05:20 AM
Post #3


Member
**

Group: Members
Posts: 350
Joined: 19-May 10
From: Byron Bay, Australia
Member No.: 11,741
Region Association: None



QUOTE(nsr-jamie @ Apr 5 2012, 08:12 PM) *

how much power did you make?


We didn't do any numbers on it as we were really only trying to get it running and stop blowing smoke. It was also proving difficult getting an accurate lambda reading, the dyno operator said it sometimes happens with certain exhaust systems.

I wasn't paying much attention to the display however I did notice the km/h reading was at 200+ a few times.

We will do a full dyno tune after fiddling about with the Webers a bit more.


Attached thumbnail(s)
Attached Image
User is offlineProfile CardPM
Go to the top of the page
+Quote Post
J P Stein
post Apr 5 2012, 06:54 AM
Post #4


Irrelevant old fart
*****

Group: Members
Posts: 8,797
Joined: 30-December 02
From: Vancouver, WA
Member No.: 45
Region Association: None



YPAF (IMG:style_emoticons/default/biggrin.gif)
User is offlineProfile CardPM
Go to the top of the page
+Quote Post

Reply to this topicStart new topic
1 User(s) are reading this topic (1 Guests and 0 Anonymous Users)
0 Members:

 



- Lo-Fi Version Time is now: 9th May 2025 - 05:25 PM