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> I musta pissed someone off, cause it just aint goin right....got the alt. out, replaced FI hoses
cwpeden
post Jun 16 2009, 08:12 PM
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Great White North, huh?
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All in one day,

Wheel bearing
Fuel leaks
Charging system
Trunk lock

(IMG:style_emoticons/default/WTF.gif)

Where do I start (IMG:style_emoticons/default/blink.gif)

I dont know, just looking for a little sympathy I guess.

I'll get started after my boys Little League game and groceries. Man I love being domestic (IMG:style_emoticons/default/screwy.gif)
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cwpeden
post Jun 21 2009, 12:49 PM
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Great White North, huh?
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Mke, What was your dilema?

Replacement Alt. went in ok. There has to be an easier way to get the bottom bolt in....Its in and the alternator is good. Turned out to be the reg. I guess.

Replaceed all the FI hoses in the engine compartment. I used 5/16 and it was pretty painless. Except for the gas getting in the cuts from doing the alternator.

Note to self...torque wheels before test drive (IMG:style_emoticons/default/slap.gif)

Next step will be CV's and wheel bearings.
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stepuptotheMike
post Jun 21 2009, 02:09 PM
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QUOTE(cwpeden @ Jun 21 2009, 02:49 PM) *

Mke, What was your dilema?

Replacement Alt. went in ok. There has to be an easier way to get the bottom bolt in....Its in and the alternator is good. Turned out to be the reg. I guess.

Replaceed all the FI hoses in the engine compartment. I used 5/16 and it was pretty painless. Except for the gas getting in the cuts from doing the alternator.

Note to self...torque wheels before test drive (IMG:style_emoticons/default/slap.gif)

Next step will be CV's and wheel bearings.


I had got the bugger back in and bolted up, but I couldn't get the bottom piece of engine tin to line up correctly. Had a big arse gap at the bottom of the fan. Went back out to the garage last night after looking at your picture and was able to get it tapped in the correct way, so all's good now.

Mike
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