I think I may have found it. First I isolated the 4 lg red wires which were bundeled. I was getting a .2a draw when these were connected to the + post. There was no draw on the starter side. Did I mention this began the day it got to 106 here? That was 3 days before it got to 113 in LA. You do the math. So this morning I hook everything back up except I used a terminal block to reconnect the previously bundeled wires
Click to view attachment Click to view attachmentand SOB; the draw is gone.
Now why in the Hell would that thing up and dissapear like a fart in the wind? Oh well! I crank the motor over and nothing. Then I remember I hadn't heard the FP run. Switch on; nutin.
After I regained my composure, I opened my copy of the FP flow chart and I traced it down to a faulty relay board.
I hope that's it and not 4 other things.