Yes I did some rerouting of the fi harness before it went in. Did a comp test before reinstalling motor.
120,110,120,125. Reinstall took 45 minutes from raising the car, to cinching the four mount bolts. It actually was quicker and easier to go in than to come out. Another two hours to hook up all connections, hoses, shift rod, clutch cable, blah, blah, blah. Fired and ran on the first turn, but hunted idle between 2 to 3K. Hmm, vacuum leak? Found one intake manifold that I had missed tightening the bolts. Fired it again and smooth as silk. That was the only thing I missed. EVERYTHING else was as it should be. Didn't even think of getting new cv joint gaskets, and the old ones were shit, so I'll get those tomorrow, and we'll be on the road.
Then as I'm doing the dance of 914 happiness, a 73, 1.7, signal orange, drives up sounding like pure shit. We had saw this guys car broke down in a parking lot about 6 months ago, and left a note on his car. He came for some help. After checking a few things and giving him the 3rd degree, discovered he had changed the pushrod seals, and failed to readjust the valves afterward. Oh boy, here we go again. I'll pull the valve covers, and see if any thing is amiss. If not, I'll do the adjustment and see what happens. It was very hard to tell him the worst case scenario.
We'll attack that on a new thread.
Thanks for all the support.
As for Brads comment about this being an inspiration: I am a cabinetmaker, not a mechanic. The last time i was inside a motor was 1980 and invloved a very simple 235 chevy six. If i can do this, so can you.
See ya in Hot Springs!!!!!!!!!!!!!!!!!!!!!!!!